Work to improve the performance and useability of
fifteen inch gauge steam locomotives
The following information has been provided by Ian Screeton the railways operations and engineering manager:-
Modifications to improve the reliability and operability of steam locomotives on the Kirklees Light Railway.
As originally constructed the locomotive fleet of the Kirklees Light Railway,
when pressed to maintain the level of service required to operate the railway,
particularly after the opening of the extension to Shelley in 1997, revealed
a range of mechanical shortcomings as well as acute limitations in the available
drawbar output inherent in the original designs.
In the light of the problems mentioned above, revealed by the intensive operation
required of the locomotives, it was considered that a number of different
aspects required to be addressed:
Firstly, the mechanical reliability of the locos needed to be significantly improved as no matter how efficient a locomotive may be, if it is not mechanically reliable it is of little use as an operating tool. Also a quite impressive amount of time was being wasted on so called ‘routine maintenance’.
Secondly, the locomotives had to be consistent performers as to steaming ability and quality of work output with a minimum level of driver/fireman input, this ultimately being of greater importance than achieving the absolute maximum drawbar efficiency.
Thirdly, an improvement in the overall efficiency of the locomotives was to be aimed for, as much to improve the output at the drawbar as to reduce the overall fuel and water consumption. Also of almost equal importance for our application of steam traction on tourist trains was the reduction of smoke and particle emissions whilst the locomotives were being worked hard up 1 in 72 gradients for lengthy periods at a time.
With this in mind and the acceptance that ultimately, to achieve truly significant
results, quite significant rebuilding will be necessary including such major
items as new cylinders, Axlebox designs with associated frame alterations
and major re-design of the whole steam circuit, a series of modifications
were undertaken. Also the fairly average performance of the original designs
meant that quite significant improvements could be made with relatively simple
modifications, of course, the closer the locomotives approach the ideal the
harder it becomes to make significant improvements in the performance.
Taking the work done by Ing. L. D. Porta as inspiration and spurred on by
the achievements of David Wardale, so fascinatingly written about in his book
‘The Red Devil’, using information and guidance courtesy of Shaun
McMahon a modest programme of improvements was started, and is still continuing
to this day. Our position of being able to manufacture virtually all that
was required ourselves, and the relatively manageable size and cost of the
work involved has helped considerably in the scope of what has been achieved,
and what, hopefully, will be achieved in the future.
Mechanical reliability.
The one significant advantage possessed by the locomotives of the KLR was
the fact that as originally built, appreciable use had been made of roller
bearings, this has more than proved to be worthwhile and is being applied
more extensively whenever the opportunity presents itself. Main axleboxes,
coupling and connecting rods were so equipped on three locomotives from new
and, with the exception of occasional damage caused during dismantling, are
still using the original bearings after up to fifteen years service (Fox and
Badger currently average 3,000 to 4,000 miles annually with 11inch diameter
drivers). Due to the limited life of the plain bearings (aggravated by inadequate
size) more extensive use has been made of roller bearings which are now showing
a real reduction in time spent on ‘routine’ maintenance, particularly
as the bearing sizes we use show very little cost difference compared to machining
and fitting a Bronze bearing. Ultimately the aim is to fully equip all the
motion work, including all the valve gear suspension links with roller bearings,
attention also being paid to better bearing sealing against ingress of contaminants.
Unavoidable wear, such as tyre wear, is progressively being reduced by the
use of more appropriate grades of materials, better detailed design and measures
such as driving wheelsets being machined larger than driven wheelsets leading
to the removal of less material when re-profiling becomes necessary.
Another area of reliability and service life which can be one of the most
expensive, insidious and time consuming is that of the locomotive boilers,
our boilers are of all welded steel construction with no formed plates other
than the barrel itself. Although the angular form of our fireboxes, particularly
the outer wrapper is far from ideal, this is not an area that has given any
trouble, so far.
Operated from new with the then company policy of not using any form of water
treatment it was inevitable that sooner, rather than latter, repairs would
become necessary. The first retubing became necessary on Fox’s boiler
(originally the most heavily used) after ten years in service, at the same
time a section of the barrel just behind the front tube plate also required
replacement due to corrosion. Only four years later the whole firebox required
re-staying, this unfortunately, falling at the same time as Badger’s
boiler became due for retubing and a similar barrel repair, culminating in
two locos being out of service in quick succession, a considerable amount
of work in only a few months and a not inconsiderable bill, even though most
of the work was done ‘in house’.
As a result of this, and having no particular desire to do it all again with
Hawk, which is now approaching its first ten years of service, it was decided
to investigate the possibility of using some form of water treatment. It was
at this time that Shaun McMahon supplied me with a copy of Porta’s paper
on boiler water treatment and after some studying it was decided to source
the appropriate chemicals and proceed with a trial application on newly re-stayed
Fox. The treatment was also intended to eliminate scaling on the internal
plates of the boiler, a problem that had not reached such serious proportions
with ourselves as on some other railways, but something still worth preventing,
the treatment was also intended to progressively remove old scale deposits.
This last was something that would require close monitoring as it had been
noted in other applications as causing considerable build up of loosened scale
around the foundation ring and associated problems requiring, initially, frequent
washing out.
Despite a quite extensive list of potential problems highlighted by Porta,
causing some considerable amount of water analysis and monitoring in the early
stages of application, the system worked remarkably simply and effectively
from the start. The only minor problem was caused by the recommended antifoam
being unavailable, and the substitute not being quite as effective as the
manufacturer claimed, the dose included in the mixture had to be doubled from
that originally advised after a brief bout of priming. The routine application
consists of the drivers simply adding a pre-measured amount of treatment every
time water is taken and that is it.
The end result after two years of use is regular blow downs are eliminated,
only being required after significant periods when the boiler water chemistry
becomes concentrated enough to override the effects of the antifoam (usually
around thirty to forty days in steam), washout periods are extended to basically
the annual inspection (around one hundred and twenty days in steam) and the
boilers are now internally very clean, as commented on by our boiler inspector.
Consistency of performance.
Upon completion of the railways extension to the ultimate terminus of Shelley,
making the total length of run 3 ½ miles with a gain in height of some
220 feet, the reality of operating an hourly service over the full length
of the line became suddenly very harsh. The time, effort and fuel required
to clean the hard pressed fires every second trip, with clinker covering the
entire grate, pieces too big to fit through the firedoor, and barely five
minutes lay over at either end it was quickly realised that something had
to be done. The rapidity with which things could go ‘pear shaped’,
particularly with drivers of varying ability, under such conditions had to
be experienced to be believed!
The overall improvement in output consistency sought was obviously going to
require a wide ranging scheme of work, simply attacking the firing problem
was not going to achieve the necessary results, particularly as the locos
where being pushed harder than ought really be required. Coincidentally it
was around this time that David Wardale published his seminal book on the
work he carried out in South Africa and this provided the inspiration and
much needed technical information for the modest level of progress made so
far with our locomotives.
The first step was to incorporate a basic form of Porta’s Gas Producer
Combustion System (GPCS) where steam, mostly from the cylinder exhaust with
the remainder made up from the air pump exhaust and blower, is fed in under
the fire and is drawn through the firebed along with the primary air, cooling
the fire to below the temperature at which clinker forms, in an endothermic
reaction, which produces combustible Carbon monoxide and Hydrogen gas (producer
gas). This gas is thoroughly mixed with more, secondary air, above the fire,
where it is burnt cleanly with no smoke and a minimum of excess air, this
fact of admitting the majority of the air required for combustion above the
fire also means there is significantly less gas rising through the firebed
to entrain and carry away small coal particles. This last is what gives the
GPCS such an increase in efficiency over conventional combustion at high rates
of steaming, but at the rates we normally operate at the overall improvement
in efficiency is quite marginal, the more significant advantage in our application,
as well as the almost total lack of clinker making the daily operation of
the locos much simpler and reducing losses due to fire cleaning, is the very
real reduction in char throwing and smoke, particularly when operating open
carriages on a continuous gradient.
The physical alterations required are remarkably simple, although there is
no denying that hollow stays in the firebox sides would significantly improve
the turbulent secondary air mixing over the fire, our present system of directing
the secondary air through a group of tubes on an air box welded to the inside
of the firedoor works remarkably well, helped considerably by the relatively
large door area in relation to the grate area and the deep fireboxes. The
steam supplied to the ashpan consists of approximately 8% of the main cylinder
exhaust led via a pipe direct from the valve outlets through a changeable
restrictor to a perforated pipe alongside the primary air opening where it
is mixed evenly with the incoming air to the underside of the fire. This is
supplemented by the air pump exhaust being fed into the supply pipe upstream
of the restrictor, part thus providing a fairly constant background level
of steam to the fire whilst the remainder is exhausted through the main blast
pipe, this supply also reduces the amount drawn from the main blast while
running without significantly increasing the steam/air ratio. Also a small
supply, about 20%, is led from the blower valve to ensure that whenever the
blower is used there is always an adequate ashpan steam supply to avoid clinkering.
Simultaneously incorporated with the GPCS were alterations to the draughting
of the locomotives, partly to compensate for the loss of available steam for
drawing the fire because of the supply taken to the ashpan, and also as a
means to reduce the exhaust back pressure at the cylinders to aid in increasing
the cylinder efficiency and thereby reducing the steam demand, and hence the
load on the boiler and fire, for the same work output.
Unfortunately due to the then stipulated constraints of working within the
existing chimney profile a less than satisfactory arrangement of Lempor type
exhaust was arrived at. This included a multiple jet blast nozzle, converging/diverging
nozzles were settled on after some basic tests with a 1.1 to 1 exit area to
throat ratio in comparison with simple converging nozzles. A large radius
entry section to the chimney was incorporated and a tapered diffuser section
taken to the absolute limit of the chimney wall thickness, resulting in an
increase of exit area of some 56% on Fox and Badger and 80% on Hawk. The end
result was an increase of blast nozzle area of around 25% whilst still maintaining
more than adequate steaming despite a loss of 8% of the exhaust to the ashpan
and the necessary increase in firebox turbulence requiring a greater smokebox
vacuum.
Latter work involved some improvements to the steam circuit and alterations
to the valves and cylinders where possible within the limitations of the existing
components with the aim of further reducing steam consumption and hence the
load on the boiler, also simultaneously increasing the available output from
the locomotives. Latter still the cylinder insulation on Fox was significantly
improved, an easy matter when it was totally lacking to start with! The reason
behind this was to reduce condensation losses in the cylinders as much as
possible, tests on stationary engines in warm still air showing up to fifty
percent of steam admitted being lost to condensation, this last work alone
making a noticeable difference and similar work is planned for Badger as soon
as practical.
A problem that has handicapped the operation of our locomotives on the relatively
steeply graded line has been the question of adhesion, or lack of it! In poor
conditions, which are not infrequent when operating a year round service,
conditions could become severe enough to stall Hawk, a total adhesion loco
of some considerable weight, prior to the fitting of effective sanding equipment.
Riding on the front of a locomotive, holding on to the lamp bracket with one
hand and sprinkling sand on the rails with the other, Darjeeling style, has
to be experienced!
Initial attempts with traditional gravity sanding proved very unreliable,
a combination of fifty percent reverse running throwing water up the sand
pipes, and severe cross winds on the exposed embankments carrying the sand
away before ever reaching the rail head, made the whole exercise pretty futile.
A more concerted effort to solve the very real problem resulted in our present
system of steam sanding, which, despite it’s remarkably simple design,
has proved to be very effective and robust, requiring zero maintenance and
working every time without fail. The system was first fitted to Fox around
twelve years ago and is still as installed, only ever being removed and inspected
if required to gain access for other work such as wheelset removal. An extra
benefit is the very small amount of sand actually used as it is placed directly
between the wheel tread and the rail at the point of contact and so very little
is actually wasted.
More work on the adhesion problem is still pending as soon as time permits,
such as rail de-sanding jets behind the driving wheels to clear the drag inducing
layer of sand off the rail head before the trailing load passes over it, the
last thing you really needed in conditions of poor adhesion is more resistance
behind the drawbar, this is one of Porta’s ideas also used by David
Wardale in South Africa. Another idea of Porta’s is to use steam jets
to ‘wash’ the rail head clean of contaminants ahead of the driving
wheels, adhesion on a CLEAN wet rail being almost as good as a dry rail, this
idea is attractive for many reasons, not least of which is you are not going
to run out of working medium and it also eliminates the abrasive sand particles
getting carried into bearings and wearing surfaces.
Closely related to the adhesion problem as well as time spent out of traffic
for ‘routine’ maintenance is the question of tyre material and
profile, time between turnings can be reduced not only by the obvious solution
of optimum material but also by such devices as Porta’s ‘high
adhesion’ profile keeping the tread clear of the area of the rail head
likely to be most contaminated and also preventing contaminants from the locomotive
itself finding their way onto the tread, reduction in wheel slip, even if
undetectable, all contributes to reduction in wear. Even the most obvious,
but often overlooked problems, such as directing excess axlebox lubrication
away from the wheels can have a very real effect, along with ensuring drains
and similar sources of contaminants are directed well away from the rail head.
Other ideas, such as machining the driving wheelset slightly larger than the
driven wheelsets to offset the increased rate of wear on this axle and combat
the ‘micro’ slipping that occurs every wheel revolution, help
maintain a more even grip throughout the period between turnings, instead
of the usual decline, often largely unnoticed, connected with traditional
maintenance methods. All the above mentioned ideas are gradually being incorporated
into all of the railways locomotives as the opportunity presents itself although
it is expected to be some considerable period of time before all the predicted
benefits become fully apparent.
Thermal efficiency.
Although an improvement in thermal efficiency was not the primary aim of
the development work on our locomotives it is an integral part of the ongoing
progress, as any improvement in efficiency, as well as being seen as a means
of reducing fuel and water input for a fixed output, also increases the locomotive
output for a similar energy input.
Many aspects of the work so far achieved, and still to be achieved, have a
significant impact on the overall efficiency and output of the locomotives,
the individual steps achieved so far, even the smallest, cannot be seen in
isolation as each interacts with all the others creating an overall impact
on the locomotive performance. Even areas that previously have been completely
ignored, such as complete cylinder insulation and far thicker insulation on
the whole of the boiler all have their part to play alongside more obvious
areas such as improved cylinder and exhaust design, all combining to increase
the overall thermal efficiency, resulting in more work at the drawbar with
less coal input to the fire.
Even though the process of development is ongoing and will probably never
reach an ‘ultimate’ point, the progress so far achieved has made
a positive impact on the operation of the railway with a significant reduction
in the amount of time spent on maintenance, more consistent locomotive performance
with appreciably heavier loads and a cleaner, more ‘open coach’
friendly level of emissions. Whilst the existing designs will continue to
limit how much can ultimately be achieved there are still significant improvements
to be made, and given a blank sheet of paper a completely new design could
show even bigger advances beyond what has already been achieved. At this point
in time our locos are far from being the ultimate expression of a ‘modern’
steam locomotive but are starting to show promise, and hopefully in the not
too distant future will be able to demonstrate what can truly be achieved
with modern steam traction in the traditional format.